POLLUTION CONTROL THAT PAYS ITS WAY
by Martin Decker, Prakash Naik & Mike Worrall Reprinted from INDUSTRIAL WASTES
Through the installation of an activated carbon technology recovery system, the Armak plant in Marysville, Michigan, is
able to consistently meet air emissions standards as well as recover a significant amount of solvent used in its tape
manufacturing operations.
Various processes were conceptually evaluated with the above objectives in mind. This survey took two months. The
processes studies included:
Condensation: An activated carbon technology recovery system solves an environmental problem and represents an economical return
on the investment.
Armak's ability to continue its tape operations at Marysville, was contingent upon its air emissions being in compliance
with the Michigan State EPA requirements. The State Implementation Plan mandates installation of "Reasonable Available
Control Technology (RACT I)" on existing pollution sources. For tape manufacture and other similar operations, RACT
limits emissions to 2.9 lbs of volatile organic compounds (VOC) per gallon of coating mix applied.
Armak's Central Engineering evaluated the technologies available to solve the problem and decided to purchase an AMCEC
activated carbon technology recovery system. This article summarizes the background of the problem and how an economic
solution was implemented.
In the tape manufacturing operation, solvent based coatings and adhesives are applied to a continuous web of material,
after which the solvents are evaporated leaving the pressure sensitive tape. Solvents are evaporated from the tape in
the initial stages of long tunnel ovens and these solvents are exhausted to the atmosphere as dilute vapors at
concentrations of about one-quarter percent by volume in air, which is safely less than the lower explosive limit.
It was estimated that the solvent laden air volume exhausted from the solvent drying stages of the various ovens was
125,000 standard cu. ft. per min. containing a mixture of hydrocarbon solvents at a max. rate of 3,750 lbs. per hour.
In addition to the environmental aspects involved, Armak was concerned with the rapid increases in solvent prices
experienced in recent years, as well as with the future availability of solvents due to the projected worldwide
shortage of petroleum products in the future.
Corrective Processes Evaluated
This involves cooling of solvent laden air (SLA) to below the condensation point. The relatively low concentration
of solvents in air requires cryogenic temperatures resulting in high energy costs (electrical power) and, hence,
poor economics. Furthermore, recovery by cryogenic condensation will condense and freeze water vapor from the air
stream requiring complex exchanger thawing techniques.
The System Being Used
The solvent recovery system is designed to continuously process up to 125,000 SCFM of solvent laden air exhausted
from the solvent drying zones of various coating lines. Four adsorbers, each containing a bed of activated carbon
pellets, process the SLA such that the adsorber exhaust solvent vapor content is reduced to less than 50 ppm - more
than 97% reduction.
The SLA has to be cooled to the optimum adsorption temperature of 100oF before entering the carbon beds. Cooling coils
fed with cooling tower water air mounted in two air-tight houses. Ahead of the cooling coils are filter elements which
remove particulates such as paper dust and viscous oil like droplets (high boilers) found in the SLA. These filters
protect both the coils and the carbon beds from the particulates.
Each filter/coil house feeds to a centrifugal fan which blows the SLA through the adsorbers. The fans are each designed
to handle half the total SLA capacity. Each fan is directly driven by a large explosion proof electric motor. Both fans
have variable inlet vanes, with automatic actuators, to adjust the fan performance to that required by the suction
controls. The variable inlet vanes reduce fan power at lower than design air flow, thus conserving electrical demand.
There are four horizontal cylindrical adsorbers. Each of the 12 ft diameter adsorbers is 47 ft long and contain a deep
bed of 43,000 lbs. of CECA-AC35 activated carbon pellets. Horizontal static beds of carbon pellets are used in all AMCEC
adsorbers, since the concept has been proven to protect the carbon pellets from attrition. Also, the adsorber design
ensures even distribution of the SLA, thereby providing high adsorption performance with low regeneration energy needs.
In the adsorbers, the carbon pellets are supported by an expanded Incolloy 825 mesh. Incolloy was selected because of
its known resistance to sulfuric vapors, chlorides and the galvanic cell that may form between carbon pellets and the
vessel wall.
A simplified flow diagram shows the adsorption and desorption phases (see Fig. 1). This depicts four adsorbers with
three in parallel adsorption phase while the fourth is being steam regenerated.
Fig 1- A simplified flow sheet : two vessels adsorbing, the right hand unit is being steam desorbed
The SLA is processed by three adsorbers operating in parallel adsorption service in a staggered cycle. When an adsorber
is fully charged with solvent, it is regenerated (desorbed) by the counterflow passage of live steam. The steam heats
the carbon to about 220oF causing release of the solvent vapors from the carbon pores, and these are carried as a
steam/solvent mixture to the condensing station. There are two heat recovery condensers which recover much of the
heat in the steam solvent vapor for use as hot water for process heating and boiler feed. The final exchanger uses
cooling tower water to remove that heat which cannot be used by the Armak plant. The process condensate separates in
a gravity decanter into solvent and water phases. The solvent, after quality control tests, is pumped to the storage
tanks for reuse in the process. After neutralization, the aqueous phase condensate is added to the evaporative cooling
tower as make-up water.
A special feature of this plant is the use of the unique AMCEC recycle loop, which cools the carbon bed after desorption
steaming. A small flow of SLA passes through the hot adsorber taking heat and steam vapor to the condenser, and then
discharges it to atmosphere via another adsorber. This loop improves the plant's adsorption performance by ensuring
that the carbon bed is properly cooled prior to reentering adsorption service. Also, the recycle loop substantially
reduces the visible water vapor plume which is normally emitted from a carbon adsorption system after each steaming,
thus avoiding possible complaints from neighbors.
To minimize operator attention and to maximize performance, the solvent recovery system is furnished with modern
controls including a programmable controller (PC). Among the PC functions is sequencing of the adsorbers through the
various process stages. All automatic valves are continuously monitored and, in the event of valve malfunction, the
PC identifies the valve. An analyzer monitors the SLA exhausted from each adsorber and, when a carbon bed is fully
charged, its steam regeneration is initiated. The analyzer loop avoids premature regeneration of the adsorbers,
ensuring effective use of desorption steam. Another function of the PC is to monitor operation of the coating lines
and only connect coater exhausts to the solvent recovery system when a web is being coated. This avoids unnecessary
processing of SLA, thereby saving fan power and dilution of the solvent air which would reduce adsorption performance.
At reduced coating loads, the PC stops one SLA fan and takes an adsorber out of service.
Automatic controls mean that the whole system - collective ductwork, solvent recovery, boiler unit, cooling tower,
solvent pumping, etc. - requires less than four hours attention per shift, most of which is monitoring, routine
inspection and quality control.
The battery limit solvent recovery system was conceived, engineered and installed in about 18 months at a cost of
$2.7 million. This price included process and equipment design, equipment supply, foundations, erection, electric
wiring, controls and thermal insulation. The system was commissioned in the summer of 1982 and performance testing
was completed within a few weeks.
After nearly a year's operation, working 24 hours a day, 5 days a week, the system is consistently achieving or
exceeding its design specification. The emissions from the whole site has averaged 0.9 lb. VOC per gallon of coating
which is well within the applicable EPA requirement of 2.9 lbs. VOC per gallon of coating. The overall performance,
in terms of recovery and utilities consumption, is summarized in Table 1.
The main operating costs of the unit - natural gas (for steam generation), electricity, water and chemicals for
treatment of boiler feed and cooling tower water are summarized in Table 2.
Recovery and Utilities Information on the Marysville Tape Plant
| Design | Actual | |
|---|---|---|
| Adsorption efficiency, recovery unit (%) | 97.0 | 97.7 |
| Overall site recovery of solvent (%) | 75 | 80 |
| Steam consumption (lbs/lb recovered solvent) | 3.2 - 3.5 | 3.3 |
| Power consumption (kw/1000 SCFM) | 3.5 | 3.3 |
TABLE 2
Operating Costs of the Solvent Recovery Facilities (1982 basis)
| Natural Gas | $0.18/gal recovered solvent |
| Electricity | $0.12/gal recovered solvent |
| Water | $0.01/gal recovered solvent |
| Chemicals | $0.01/gal recovered solvent |
Conclusions
The recovered solvent is of acceptable quality and is recycled back to the process without further treatment.
There is no evidence of carbon pellet contamination. Some high boilers are being condensed at the SLA cooling stage.
To date, no corrosion has been experienced. The pH of process condensate is 4.8 to 5.0, which is higher than expected
and therefore, anticipated corrosion of the equipment is unlikely.
No more than normal maintenance has been experienced, and the unit has been operational more than 99% of the time
that the coaters have been working.
The system has more than solved an environmental problem and represents an economical return on the investment.
At design conditions, some 15,000 tons per year of organic solvents could be recovered for reuse.
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